Hi Guys,
Some may remember that we repaired both of Carling's upper and lower bushings (car stuck in Reverse, crawl underneath and shift it manually, drive it home and stick in a new teflon piece) and tied each connection up with lockwire. It worked fine for about 6 months, but last month in Sarasota it popped out of the bushing again on the top end. Pulled out the shifter, popped the connection back into the bushing, tied it up with wire, but now I don't trust it. Sigh...
Now my Lord and Master the Engineer has a new fix in mind--putting a bolt through the whole thing. Has anyone tried this?? How long are other people's fixes working?
Trice
1968 280SL US, signal red/bl leather, auto, kinder
Sarasota FL; Alsace France