Hi guys, Well the engine is now out and sitting on the garage floor, Hurrah. However, it was much more fiddly than I thought it would be and I can see it being difficult to put back. The problem I had, apart from doing it on my own, was that the unit kept fouling the throttle linkage on the bulk head. To get past this I had to increase the angle of the engine but couldn’t do this until the gearbox had cleared the steering linkage as the engine wouldn’t go far enough forward to allow the head to stop fouling the rear bulk head and throttle linkage when lifted, hope that makes sense. Anyway after much jacking/lowering/lifting/everything else and a considerable amount of force on the throttle linkage it eventually came out at the required 45deg angle. After all that, my point is, is it normal to have such a fight with the throttle linkage or have I missed something in the process. All round, it would have been much simpler to have removed the head which I think I will do when putting everything back in.