Hi Dan
Well, I am trying to do this as a project that won't cost double as much as a regular rebuild, so I have done a lot of research and also gone back to my old school books (I studied engineering for 8 years at the Technical University in Berlin), which have been less valuable than common sense and the practical knowledge that I'm acquiring.
Yes, the pistons are all fairly close to deck height, like I said, 24 thousanths in. below deck on the 9.5 engine (late 280SL) and 40 thou. on the late style 280SE engine (I don't like using inches, but it looks like you did below and most people here relate better to those numbers). I also have calculated how much I'd have to take off the top of the pistons in order to lower the compression ratio back down to acceptable levels after the 5mm/ 0.2in. stroke increase. Using the stock pistons and rods on this trial run, I did not feel comfortable removing as much as I wanted to without making the top (crown thickness) too thin. So, my piston will be travelling all the way to level deck height, whereas stock, TDC was 40 thou. below deck. It turns out the lower compression head off my donor SE engine actually works in my favor with the compression ratio, even with lower compression height of my machined pistons.
I found a reputable company with much experience in "stroking" an engine by welding extra material onto the crank journals that will then be re-ground to give me the increase in stroke. Ultimately, I will probably use custom pistons with 3 instead of the standard and conservative (not to say old-fashioned) 4 ring design used on M130 engines. Of course, custom pistons would be lighter weight and stronger. They also balance the crankshaft with the lighter pistons, flywheel, balancer... I don't feel like the bore should be increased beyond the 87.5mm maximum repair size because of the already thin walls between the water jacket passages.
As far as the head, I am still open to suggestions. Eventhough, I am not adverse to experimenting, I know enough to realize that without much experience and computer aided modelling and bench testing, more harm than good can be done by just increasing everything within the head. The valves are already fairly close to the edges of the combustion chambers although I would love to hear about any 1mm larger, drop in valves with the same valve stem diameter. Obviously, some matching and porting can do no harm, since I will have a 3 liter engine that should require proportionally more air and fuel than a 2.8L. Again, I'd be glad to hear about experiences with extrude honing (how much will that do? ...an increase in port diameters, only to have the restriction be moved to the intake runners?) and other modifications. I'm sure there are some on this list who have experience with this and who don't have a problem with me doing some respectful (hopefully respectable too) work on an MB engine. As I am otherwise a stickler for strict originality, I am only considering modest internal engine changes (no V8s or turbos) and I want to be able to use 91-92 octane (US) gas. (02 cam, modified pump mapping and head work.
I tried to attach pictures of the two different combustion chambers for feedback, but always got a message that I was not signed in....?
Tom Colitt