Glad to here your back on the road.
87.5mm is second repair, i had mine bored out to this size and fitted second oversize 87.5mm pistons.
Confusion over part numbers lead me to order the wrong gasket twice, i believe its one of the reasons it failed, that plus the fact the head had been previously machined down to 83mm which would raise the compression.
Further to this the water ports still have corrosion around them which didn't help and i cant skim the head any further.
I have sourced another head at stock 85mm which i intend to weld build up any corrosion around the water ports and skim to a perfect finish. Hopefully this combined with the correct 87.5mm gasket will solve my problems.
Im working crazy hours at the moment but intend to sort this work out mid July to allow me back on the road for August.